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- Large pockets added to the face to reduce weight. The thickness in these reduced areas is now 0.050".
- Material in the center section was removed completely.
- Internal radii were increased increased from 0.0625" to 0.125". This increases strength and is more fitting for our tool availability.
- The rim thickness is decreased to 0.0625" in areas that do not have tapped holes.
- The large 0.875" dia hole was replaced by four holes that house connectors that will better organize the wires that pass through.
- The material was changed from 6061 to 7075-T651.
Creating Blank
Waterjet stockThe stock was waterjet out of a 12" x 12" x 1" plate of 7075 aluminum.
Payload Bulkhead Stock Rev3.DXF is attached. This is the file that was used to waterjet the octagon blanks.
The stock was cut with 16 sides instead of 8 sides to reduce the amount of turning that would need to be done after the milling operations..
After the blank profile was cut, two opposing faces were cleaned up on the mill. Holding the blank in the vice with these surfaces, the largest faces were faced and checked for parallelism.
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Preparing CAM
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Milling
The toolpath was created using HSMworks from the Solidworks CAD file.
The tools used in the CAM included:
0.5" flat endmill
0.25" ball endmill
centerdrill
1/8" flat endmill
The estimated machining time was 58:52
Milling
This part was machined on a CNC mill in The Deep
The stock was clamped in the vice and the origin was set to the center of the part using an edge finder. After the tool table was created and the Gcode file loaded, we tried to run the operation, but the Z axis was not moving. We noticed that the machine was set to 2 AXIS mode which caused this problem and switching to 3 AXIS mode solved it.Machine was set to 2 AXIS mode which caused the machine to not move the Z axis while cutting. The machine was changed to 3 AXIS mode and this solved the problem
Turning
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Radial Indexing
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