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The solid rocket propellant [Name TBD] Deimos, previously called "Propellant XBlue Voltage" in development, was developed after the COVID-19 pandemic for Project Medusa with initial mixing and testing in April 2023 and finalized in September 2023.

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History and Purpose

After the successful manufacturing and launch of Phoenix in January 2023, the team created goals for the next Spaceshot rocket, Project Medusa. One of the Medusa goals are to get halfway to space (~185,000 feet). ThereforeDue to the performance of Angry Goat in Project Phoenix, it was clear that a new propellant was necessary to fit the project's goals. Initial propellant formulas were developed in spring 2023, and characterization tests occurred throughout summer 2023. Lack of AP access slowed down the process in late summer -early fall 20232023-mid winter 2024. Deimos is just barely pourable enough to be considered easily handled. Any more dense and it would not be pourable and would need to be packed.

Goals for this formula:

  • Higher packing density than Angry Goat, but not so dense it becomes difficult to pour like Cherry Limeade
  • Higher ISP than Angry Goat
  • Experiment with trimodal AP
  • Experiment with burn rate modifiers

Changes from previous propellant (

...

Angry Goat):

  • Use of smaller AP particles than Angry Goat
  • Removed Magnesium
  • Experiment with trimodal AP
  • Experiment with burn rate modifiers
  • Replaced HTPB with a new bonding agent to combine HTPB and Tepanol bonding agent
  • Increase liquid content slightly to mitigate packed density

Formula

Ingredient% Mass
HTPB w/ CAO-5 & HX-75211.369%
IDP5.344%
PDMS.050%
5 µ Al Powder9%
200 µ Ammonium Perchlorate48.355%
90 µ Ammonium Perchlorate24.178%
MDI1.704%

Performance and Combustion Properties

Density: 0.059740 lbs/in^3
a: 0.020550 in/s
n: 0.376100
Typical ISP: 210s

Mixings

DateDesignationMotor(s)SiteResult
4/17/23Baja BlastCharacterization MotorsRT LabResulted in too low pressures
7/23/23
Blue Voltage
DeimosCharacterization MotorsRT Lab
      

 

Acceptable grain; static fired and used for characterization
12/5/23DeimosCharacterization MotorsRT LabSame result as 7/23/23 mix







Static Fires & Flights

Date

Propellant

Result
7/1/23Baja Blast

5 test motors integrated: 2 successful fires, 1 failure (igniter lodged itself inside the small nozzle opening), 1 didn't ignite (igniter was well at the bottom but the motor, 1 not attempted (nozzle was smaller than the failed motor, so even higher risk of repeating failure). Unfortunately, we couldn't use this data due to our pressure numbers for static fire being lower than expected (to the point that it's an issue). Likely issue was due to our load cell because hydrosttic test was successful (so no leaks).

7/15/23Baja Blast

Static fire cancelled due to thunderstorms all day

7/29Baja Blast

Two successful fires, but both motors had leaks, leading to substantial pressure loss. Location of leaks weren't clear until de-integration: the braces pushed the nozzle away from the carrier by a few thousandths, destroying the RTV seal.

Decisions after this static fire: create new formulation for next characterization fire, and remove converging section of nozzle (make it a graphite puck).

8/29
Blue Voltage
Deimos

5 test motors prepared, all successfully fired. Pressures are within good operating range (Nozzle A - 1779 psi, Nozzle E - 1249 psi, Nozzle I - 1283 psi, Nozzle, N - 808 psi, Nozzle S - 684 psi 

Interesting observations about all motors:

  • minimal slag (not enough to make full rings on any motors)
  • nozzles weren't flush against forward retention ring (FRR) bolts before firing, but were flush after firing. All but nozzle E had O-rings pushed out around part of the nozzle that sheared
  • nozzles had signs of cracking around them, with nozzle N shattering entirely
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